Saturday, 13 September 2014
New Main Hatch Garage
I have been busy last week making a new hatch garage. The old one was getting worn, but more importantly could not stand the weight of a man as heavy as myself when stood on! The rebuild has also given the opportunity to add a flat facia on the aft edge of the garage where a small Standard Horizon chart plotter can be installed.
An extract from the Survey and some of what I have been doing!
Survey Requirements from Sept 2011
RECOMMENDATIONS
The following items in need of attention or comment were noted; to assist in their evaluation they are divided according to the categories:
(A) Items requiring attention as soon as is practicable
(for structural or safety reasons)
(B) Items which will require non-urgent attention in course of maintenance
(e.g. to rectify defects or to inhibit deterioration in future)
[Note: Recommendations are intended as a guide only, and further information can be provided if required. Additional suggestions concerning minor items of routine maintenance or improvement may also appear in the main section of the report, but are not intended to be comprehensive or exhaustive in this respect (e.g. cleaning and repainting, general maintenance and servicing). Items or areas where some deterioration is evident but which do not necessitate remedial measures at present are also included in the main body of the report, with a recommendation for monitoring periodically in future.
Recommendations in section (A) should be carried out as soon as is practicable, whilst those in section (B) may be fitted into a normal programme of maintenance to be completed within the next year or so (unless another time scale is suggested within the report – some recommendations require the vessel to be ashore, or would be easier to attend to in this condition). Routine actions such as obtaining a new licence for the VHF radio are also included within the report.]
(A) Urgent requirements
1. Free off and service cockpit drain seacocks, and improve access to them in future. (See A.6).
Two new blakes seacocks installed 2014. New cross over hoses and clips to new cockpit sole drains with inspection hatch. New teak grate over.
2. Tighten the connection of the engine‟s fuel delivery pipe at its union with the engine-mounted fuel
lift pump, and re-secure the union of the armoured hose and copper tubing nearby. (See F.3).
Completed in engine service 2014
3. Remove the mainsail cover in order to repair its detached zip tabling and thus enable ready access to the mainsail. (See A.5). Completed before purchase delivery 2011
4. Strap batteries in position to prevent any possibility of movement in extreme conditions. (See H.1).
Completed in 2014 – batteries now in plastic boxes
5. Ensure that safety equipment appropriate to the intended use of vessel is carried on board when yacht is in commission (e.g. in-date distress flares, additional fire extinguishers, etc.). (See G.3).
EPIRB and Liferaft added in 2014. Extinguishers new in 2011. New carbon monoxide and smoke alarm
B) Requiring attention
6. Carry out further investigation of condition of screwed plank fastenings at garboards and below-waterline hood ends, anticipating the need to renew most of these as a precaution (estimated about 80 in total). (See A.4) Completed by Kings in 2013
Also carry out further investigation of the condition of strap floor bolts by removing samples for inspection, and reinstate the missing or corroded bolt found aft on port side (this will require removal of the engine and its drip tray for internal access). (See A.4).
Completed by Kings in 2014 – All strap floors regalvanised apart from the one under the negine which was epoxies and the one under the forward bunk that required cabin furniture destructions to gain access.
7. Renew the copper tingle over the starboard side of the rudder‟s tie-bolt gallery. Secure the tiller to prevent movement in the tiller hood, and to ensure that no moisture ingress into the tiller‟s timber occurs. (See C.1).
Completed in 2014 - new Ash tiller 2014 - old one being repaired and will act as spare
8. Clean off superficial rust from some fittings, wherever found (e.g. strap floors, quarter knees, engine mounts, etc.). (See A.3, F.1).
Completed in 2014 – and repainted white for leaks to show more easily in future.
9. Tighten the wind generator strut stays to limit movement of the strut, and improve its bracing to the sternguard. Rectify deck leaks wherever found. (See D.1, D.4, H.1, J.2).
Will complete when re installed - removed to get into paint shed.
10. Renew both perished portlight seals. (See D.3).
Completed in 2014 – Classic Marine serviced all opening ports and cleaned the surrounds of the closed ones. New armoured glass.
11. Check condition of mast fully when next unstepped, with particular attention paid to apparently minor softening in way of a graving piece inserted in its forward face close above the heel, as well as at a cleat on starboard side (also secure this cleat which is loose). Give cosmetic/protective attention to the main boom and staysail boom, particularly at their outboard ends. (See E.1).
Completed in 2014 Epoxy repair to mast. Cleats on mast rebedded. Mast Coelaned.
Main boom revarnished. New end fitting for roller reefing. Rot under fitting was consolidated with epoxy.
Staysail boom: New scarphed spruce end. New galvanised clew fitting over.
12. Rectify leakage from the seals of the manual bilge pump and galley handpump by fitting new seals. Consider the provision of a modern diaphragm-type bilge pump for easier operation. (See G.2, I.2) Completed in 2012 – new thru-deck Whale Gusher - strum fitted to intake. One extra auto electric bilge pump added for emergencies and taking up (2014) - drains through cockpit. Main auto electric pump has had a air pressure float switch fitted with new hull fitting over Port side (2013).
13. Renew the sacrificial zinc hull anode when the vessel is next ashore (not urgent). (See F.4, H.6).
Completed in 2014 – moved aft to repair softening of wood around previous bolt holes.
14. Carry out minor refurbishment within and rectification of deck leaks into the accommodation. (See J.2).
Completed in 2014
15. Provide an outboard motor bracket for the inflatable tender (if the outboard motor is to be utilised). (See G.5).
Completed yesterday!
Tuesday, 9 September 2014
Rosie in the paint tent at present
Rosie is back in the paint shed. I had too many jobs and not enough time to launch her ready for the Classic Boat festical in London next weekend. Instead I will travel down by train. There is plenty to do on the inside including some rewiring and much repainting and re varnishing. So looking at an October launch now.
Fore Hatch work
The fore hatch was basically been held together with varnish. When stripped of the old varnish the hatch just started to crumble before our eyes. So luckily, with the help of some epoxy it has held together and looking respectable covered in very generous layers of left over Coelan from the mast job. It will last out a couple of seasons but am aware that a new one needs to be made sometime in the future.
Working on the boom
This week has seen a bit of work on the spars. The clew fitting to the main boom has been redipped and the rot in the boom under it graved in. There is also a new laminated mahogany capping end. I did varnish it to a nice a shiny level, but sadly the dew got it and now it is cloudy. Sadly the season for painting and varnishing is over.
Saturday, 30 August 2014
Getting the boat back together
I have now started going down the list of essential item to get her ready for launch which is in a week or so! I decided that cleats might be nice. So renewed Burma teak needed to be carved to fit the cleat upstands. I thought it would take an hour or so each, but in the end in was two and a half hours per cleat! So that is a days work then!
Friday, 29 August 2014
Cabin Front Leak - repair in action
The leak on the cabin front is now fixed by being consolidated in epoxy and glass tape. Only a decorative beading required now.There was also a leak by the cabin ports which was wrecking the interior shellacked mahogany. We have been trying to strip the shellack but sanding is not an option as it turns into a very gooey mess.
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